stickhunter
CGN frequent flyer
- Location
- Victoria, B.C.
I recently received a box of 500+ unknown reloads that I wanted to pull so I could recycle the brass and bullets. I have a Hornady Cam Lock bullet puller that worked well-enough for the jacketed bullets, but it wouldn't budge the cast loads with a roll/taper crimp. The cast lead was so soft/slippery, that the jaws of the bullet puller would just swage the bullet down as it slipped through. I was also not relishing the noise and mess of hammering hundreds of bullets out with an inertial puller.
Since I was going to re-melt the cast bullets, I wasn't concerned about damaging them, so I decided to try pulling them with side cutter pliers. Unfortunately, my press' ram and shell holder were too short to raise the bullet high enough to grasp:
I had a 1 1/4" deep socket which ended working perfectly --- the ram could extend up the socket and the bullet came through the 3/8" drive opening where I could grasp it with the cutters:
I mounted the press temporarily on a saw horse so I could use my hip to push the handle in, lowering the ram, while I griped the cutters:
I won't say it was effortless, but it saved my hands and back, and I was able to pull about 3 bullets per minute:
A couple of rules-of-thumb that i learned over the course of a couple of hours of work:
When it was all said and done, I ended up with 11 cartridges that I just couldn't pull before the lead cut away --- those will go into the range's burn bucket.
Here's a pic of the setup I used for getting some of the really stuck bullets moving:
Was it worth the effort? Absolutely not, but I'm a stubborn person and I don't like letting things go to waste. That being said, I'd never accept another person's reloads unless I desperately needed the brass.
Since I was going to re-melt the cast bullets, I wasn't concerned about damaging them, so I decided to try pulling them with side cutter pliers. Unfortunately, my press' ram and shell holder were too short to raise the bullet high enough to grasp:

I had a 1 1/4" deep socket which ended working perfectly --- the ram could extend up the socket and the bullet came through the 3/8" drive opening where I could grasp it with the cutters:




I mounted the press temporarily on a saw horse so I could use my hip to push the handle in, lowering the ram, while I griped the cutters:

I won't say it was effortless, but it saved my hands and back, and I was able to pull about 3 bullets per minute:

A couple of rules-of-thumb that i learned over the course of a couple of hours of work:
- Arrange your workspace efficiently so you don't have to move much or bend over: I had the cartridges in my pocket and an ice cream pail to catch the powder and a shelf to place the bullet and case.
- Don't be shy taking a good bite into the bullet as it's going to be damaged anyways and your best chance at a pull is to make a good first impression.
- Don't keep struggling with obstinate bullets; put them aside and keep moving on as you want to develop a rhythm and maximize your output.
- At the end, revisit the tough bullets; I found pressing the bullet in with a vise, using a shell holder to prevent touching the primer, sometimes helped break it free for the next pull attempt.
When it was all said and done, I ended up with 11 cartridges that I just couldn't pull before the lead cut away --- those will go into the range's burn bucket.
Here's a pic of the setup I used for getting some of the really stuck bullets moving:


Was it worth the effort? Absolutely not, but I'm a stubborn person and I don't like letting things go to waste. That being said, I'd never accept another person's reloads unless I desperately needed the brass.