So last night I pulled the barrel off of a buddies new to him rifle to thread it for a muzzle brake. It is a very nice rifle, Surgeon action, match barrel, it was built buy a reputable smith. So here is the funny part. First off the barrel was on there very very tightly, finally got it to break lose and there is a ton of green loctite in the threads. Think to myself, "meh whatever not the first barrel I've seen loctited on." Clean it up, thread muzzle, install one of the GST precision brakes on it. (Nice brake, especially for the money) Before I took the barrel off I marked TDC on the barrel and the action with a sharpie so I could tighten the barrel back up to where it was and time the brake easily.
So I get the brake on, clean up the loctite and apply a bit of anti seize to the threads instead. Slap the wrench on the barrel and go to tighten it up, the weight of the wrench alone turns the barrel up to the timing mark, maybe even a bit past it. Give it a bit more to torque the barrel up and now the timing mark is at the 1' O clock position or a bit more in relation to where it was when I took the barrel off.
"Well that sucks" now I need to re time the brake, I decided to trim the brake to get it timed up again instead of lengthening the thread tenon on the muzzle.
I did not stick a go gauge in the chamber as I don't own one for 308 at the moment, I took the firing pin out an ensured it would swallow a few types of factory ammo I had here. By far not a perfect set up but it chambers fine and shot great today.
So I have been trying to figure out what happened and why it happened. My thoughts are that the original builder made a bit of a mistake in a dimension somewhere and instead of tightening the barrel all the way up they just slapped a ton of loctite on it, and turned it up hand tight and left it.
Orrrrrr, hopefully what happened is a bit more of an "honest" mistake and all the loctite that was put in there started to harden up a bit quickly and caused a bit of false torque up?
I highly doubt the anti seize created enough lube to let it over time that far on it's own.
Any thoughts or ideas?
So I get the brake on, clean up the loctite and apply a bit of anti seize to the threads instead. Slap the wrench on the barrel and go to tighten it up, the weight of the wrench alone turns the barrel up to the timing mark, maybe even a bit past it. Give it a bit more to torque the barrel up and now the timing mark is at the 1' O clock position or a bit more in relation to where it was when I took the barrel off.
"Well that sucks" now I need to re time the brake, I decided to trim the brake to get it timed up again instead of lengthening the thread tenon on the muzzle.
I did not stick a go gauge in the chamber as I don't own one for 308 at the moment, I took the firing pin out an ensured it would swallow a few types of factory ammo I had here. By far not a perfect set up but it chambers fine and shot great today.
So I have been trying to figure out what happened and why it happened. My thoughts are that the original builder made a bit of a mistake in a dimension somewhere and instead of tightening the barrel all the way up they just slapped a ton of loctite on it, and turned it up hand tight and left it.
Orrrrrr, hopefully what happened is a bit more of an "honest" mistake and all the loctite that was put in there started to harden up a bit quickly and caused a bit of false torque up?
I highly doubt the anti seize created enough lube to let it over time that far on it's own.
Any thoughts or ideas?